had quite the adventure this week.
Oh boy where do i start... it's kinda long so i'll try to go readers digest style
1. I'm dumb and let my OCC over-fill.
2. out of town helped my wife drain it over the phone
3. began hearing ticking noises like cards in a bike wheel presumed cams.
4. wife gets code p0012 VCT solenoid bank 1 over-retarded (MIL illuminated)
5. check PTS to find there is a TSB for that code with a mil. the fix is...
6. UPDATED PCM calibration with IDS (returned to stock first, all that good stuff)
7. still hearing ticking cam noises. so did some research. possibly VCT solenoid unlikely on a 2016, possible oil flow issues (okay maybe, with the catch can over-filling). or maybe just something as simple as low on oil.
8. check oil. its not even on the dipstick, it comes out splotchy halfway up the dipstick not on the end. dark brown and dirty (just over 5k miles on mobil1 0w30)
9. OH Crap, i need to add/change my oil now!
10. drain oil, maybe 2 quarts of the dirty dark brown crap comes out. (well thats weird, the book says 6 quarts i know it usually doesn't drain all 6 but dang.)
11. put on my new oil filter and ran mobil1 5w20 in an attempt to thin/even out if there was any more tar left in there. put in 5.5 quarts engine took it all no problem and dipstick read.
12. cam noises seem to subside. will probly go back to 0w30 or the recommended 5w30 after a couple thousand miles.
13. now I'm trying to figure out this oil consumption. and looking periodically. the short hose from my OCC to the manifold seems oily on the blocker thing inside it, if I pull my manifold MAP it is soaked in oil. (even my 2 bar that's only been there since the IDS PCM update) so many issues from a 2016
i've read some scary things, valve covers getting replaced, VCT solenoids, and even crank bearing issues (yikes)
all the while i've emailed torrie with my updated PCM info, and got my 89MPG and my 93PERF tunes. only problem is. i flash the 93PERF and it wont turn over. cranks and stalls says general error 21000 when i tried reading the code(s) im not sure if that's an error reading codes or an error with the car. . 89MPG works okay; didn't drive far but didn't trip any MIL. what an adventure. stock tune with the 2 bar for now.
well i tried to keep it short for you guys. I seem to always throw my issues on the wrong thread so I made this adventure its own thread, hope you guys can help...