Ok so another weird and wacky update. With all of the suggestions and info from my web searches, I decided to do a few things. #1 Installed the 3 bar sensor and 91 V8 tune. I then reset the communication codes in the PCM and reset the adaptive learning through Forscan. To ensure that I had actually reset everything possible I then followed these instructions.
https://youtu.be/hZAsoqmqhdMAnd followed his instructions regarding the learning process. Drove the car for about 2 days without doing any crazy WOT blasts and 55 mph pulls.
After FoMo's and ajp comments I decided to start logging fuel trims and dropped a few other PIDs that were unnecessary for this purpose. As I am trying to limit the total PIds that I am monitoring to keep the connection as quick as possible. So it's 8C today here (it's finally going to warm up later this week lol). Drove the car today a little more aggressively. A few WOT pulls from 0, a few WOT downshifts into second and then finally a few WOT pulls down into 3rd to 4th. It's gone, I mean completely
gone. I am still running the same fuel. I can't be happier however I am skeptical that it's truly gone lol. I will continue to be cautious over the next few days just to be safe and datalog any WOT blasts. HPFP no longer drops below 1500 PSI. However I know see the TP1 sensor modulating on a hard WOT downshift. It's not stuck at wide open. I will post a few screenshots of the data logs later showing the HPFP and the trims.
Any ideas on the results? Could the car actually needed to adapt to the fuel or conditions was there something stuck in the KAM that was contributing? This is over my head, any insight would be great.