Hey guys,
I went to run my car at the track this weekend (Sunday) expecting to run atleast 12.5 or better possibly. First run out of the gate was a 12.9 so I felt O.K, every subsequent run was in the 13.9-14.5 range, so I figured something was wrong with the car, took a look at the boost gauge, and got some logs - sent to AJP - don't have them with me at work- and it looks like the car was SEVERELY underboosting (ie. 4 psi at WOT).
I checked all of my added vacuum/boost connections due to the Tial BOV, MV-S wastegate, etc. and didnt see an issue.I started the car to let it idle, and heard an air rushing noise on the drivers side, a little near the rear of the engine bay. Took a look at the CAI, and the coupler wasnt sitting on the factory piping, there was a gap, I assumed this was the entirety of the issue. Fixed it, however there is still an air rushing sound. There is another coupler near that area, that is an OEM clamp I have never touched, and I am afraid it may be warped.
Here is a pic from google,

The clamp I am concerned about is pictured right behind the hose connector. It seems that part of it is mated to the pipe as a one-piece assembly? however on the end facing the rear, it seems warped, but when putting my hand near it I do not feel any air.
Any suggestions would be appreciated. When I am home from work, I plan to let the car cool off, then jack it up, and double check all of the charge pipe connections that I can.
Edit: added pics of how the CAI was (now fixed) and the coupler I am concerned about. After fixing the CAI connection, I can get to 10-11 psi, but should be seeing closer to 16, or at the very least 14.5 as that is what the boost regulator is set for.
Thanks guys