Just to throw this out there, but my misfire ended up being a cracked piston. Car would shudder and surge when starting up and the exhaust definitely had a very rich smell. Never had a chance to hook my Torque up to see what my ratio was...
Dealer replaced plugs, swapped coils, did a contribution balance test on the injectors, and finally a compression test showed #2 was down 19% vs the other cylinders.