ok here is two STOCK .96 OAR level logs.
EDIT :: looks like the SCT choppines is solved. smooth logs..
LOG1 :: One is the wealth of new pids i found .. including wastegate pids for the bypass and baraomoter.
i included a bunch fun troubleshooty sounding stuff. i have no idea if anyone else has anything they can help compare me to... if you have a 2010 with DMJKBLA id be curious if you logged the same pids on a 1-4th gear autopull what the diffs might be.
LOG2 :: std brad logging cfg file datalog.
now here's the fun new part. it is no longer doing the bad behavior in stock mode. in fact stock mode is way stronger than i recall it being.. wierd but ok. gives me about an inch of hope.
swapping back to my good solid tune from before the meth, off to drive the oar to .96 and get the same 2 logs.
FoMo; yeah Brad an i log the spark, knock, tqsrc. with the new pids i found i added anything that said 'safe', 'fault' or error and the usual tqsrc and knock and misfire to the new 'wth' config file.
when i get my 'tuned' OAR back to .96 i will run the same two logs i just attached with it, it is a 14psi tune with a emphasis on spark from brad.
all comments are appreciated.
this have been going on for almost 6 months so if it sounds like panic it is a mix of frustration, desperation panic and a dash of pissed off

the fact Ford has not idea whats going on is super frustrating.
I am very tempted to start tuning from scratch and get a base tune from brad and go through the basics again, see where we hit the wall. Brad what do you think?