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- Jr. Member
- Posts: 23
- Ecobooster
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I have a 2013 f150 limited and am experiencing a loss of boost pressure and turbo noise. I have recently began to notice that I have developed a negative ltft on bank 1 that load dependent will fluctuate between 10-18% It is 13% negative at idle. The other bank only goes about 3-8% negative. At around the same time I started to notice a high pitched squeel or whistle when boost climbs above 12ish psi. TIP DESD also outruns TIP ACTUAL under load with before it can catch up. Snow controller states under loads that are not WOT I can build about 16psi, which is 6psi drop from what I had before. WOT has steadily lost boost and now will only hold approx wastegate pressure (5-6psi). Intermittently getting a P0299 and P0035. truck has a turbo smart boy and factory bpv is still plugged in. I put in the BOV awhile back due to tear in bpv causing boost leak at wot. I have a stage 3 snow kit, but haven't ran it since noticed issues starting. Pcv is deleted and engine vented into a catch tank in front bumper. Basically stock otherwise, I dd truck and have very little time to work on it, so hopefully someone can start me in right area to help me get it fixed quickly. Thanks.
2013 Limited F150 4x4, OEM turbos with CRP billet compressor upgrade, Meth injection, PCV deleted and VC's vented to a custom blow by tank in bumper, Corsa exhaust, Turbosmart BOV, AEM drop in filter, tuned on SCT (93 and E30 +METH), leveled on 305 NT420's, DD
2016 Mustang GT, premium, Performance Pack, 6 speed, Lund Tuned on HP tuners
1995 Mustang GT, 347, AFR heads, custom nitrous roller cam, EFI, NX wet plate 175shot, Astro T5, stock suspension, 275 radials
1979 F250, 1970 460BB, DOVE-C heads, 850 holley, solid roller, long tubes, 10" suspension lift, trac bars, 4 speed, 42x15x15 TSL's
1989 Honda Crx HF, H22A1 swap, custom 4-2-1 header and test pipe, cable trans conversion, driveshaft shop axles, NX wet single nozzle 175 shot, trac bars, stripped, 1800#'s